One thought on “Better Luck Next Year”

  1. In the plans We had 35% hover duration time margin.
    We has a 25% peak thrust Margin

    We just never got the mixing to happen correctly. We were at about 60% of the theoretical ISP and we still had enough performance margin to do the task, but with that low of ISP we did not have the flow in the main injector orifices to get the chamber pressure up where it needed to be to lift off.

    Even 70% of theoretical ISP and we would have been good enough. I needed to pay more attention to the weird pressure pulses and nonsensical
    chamber pressure readings earlier on in the project.
    I just assumed that while it was suboptimal I had enough margin.

Comments are closed.